Me and My ASP Pt. 4: She’s Finished!
The ASP is done! Last Thursday I rolled the car in the trailer and headed for Gingerman Raceway on the west side of Michigan but not before taking a few photos that Harlo posted here last week. My good friend and famed photographer Fabrizio Costantini also came by to take some beautiful photos as well.
I arrived at the track late in the afternoon to shake the car down at their test and tune night. I got to chase around several other open-wheeled cars of various formula. The ASP felt like an old familiar friend and it handled better than I remembered. It might have something to do with changing the geometry of the tie-rods for better bump steer and definitely has something to do with calling over Garret Van Camp (the set up maestro) to help me dial in the camber and toe. I took it pretty easy as I made about 10 laps around increasing my speed with each lap, seating in the new piston rings.
The car felt good, sounded good and then after about 20 minutes of remembering why I love FV so much something went amiss. I couldn’t seem to find any gear other than 4th, so i pulled into the paddock to find out what was going on. A broken shift rod was what was going on. Upon further inspection, it appeared to be made of paper thin steel tubing that must not have held up to the nickel plating process. Perhaps it’s the one part on the car that was designed by Collin Chapman to be as light as possible. I was done for the day. The next morning I began my quest to find some adequate steel to remake a part that would last. I found a steel supplier conveniently located a few miles from the track and the guys at Trackside Motorsports which is as the name suggests is conveniently trackside. They assisted me in remaking a new and improved shift rod that had me back in action for Saturday’s qualifying session.
It is my hope that the rings are still seating and that is what landed me 11th on the grid out of the 30 cars but in truth it was probably some combination of my time out of the car, the rings and the stiff competition. The car did seem to make more power as the weekend went on though… or at least I imagined it did. For the start of the race on Sunday I got away quickly and managed to get around 3 cars before turn 1. By the 3rd to last lap I had made my way into 5th place but then was passed back by Guy Dennehy. I stayed on his gearbox for the next lap hoping I’d be able to draft around him on the back straight. As we came up to the Turn 5/6 combination he went in a little too hot and back end of his Lynx started stepping out and I sensed he was going to lose it.
The car spun left and I went right, then he tried to correct and it snapped back across the track in front of me and I went waaayyy right off the track (as to not spear my pal Guy). I tried to not give the wheel any sudden input and edge it back toward the track surface but as has happened so many times before when two wheel are on grass and two on pavement, my car too snapped into a spin. Most every car I’d worked to get around, got around me in an instant, and several of them too close for my comfort… I had a front row seat to oncoming racecars. As soon as the last car went by I whipped around in anger (just an expression) and started trying to chase down the pack. With only 2 laps to go I knew it wasn’t likely but my heart was pumping and my tires were sticking. I passed all of the lapped traffic before the last lap and had Guy and the rest of the pack in my sights but they had just made up too much ground. If I’d had one more lap who knows. I finished lucky 7th, feeling lucky that I could roll the car back on the trailer unscathed to fight another day.
See the complete restoration story here.
Stay tuned for details on the next project which is nearing completion… a 1969 Merlyn MK11A Formula Ford.